Four important bolts were missing from a Boeing 737 Max 9 that lost a passenger door plug during flight, the National Transportation Safety Board concluded in its investigation.
The NTSB's preliminary report issued today is consistent with earlier news reports stating that investigators believed the bolts were missing when the plane left Boeing's factory. The plane used by Alaska Airlines was forced to make an emergency landing on January 5 when the door plug—which is used instead of an emergency exit door—blew off the aircraft in mid-flight.
An absence of markings around the holes where bolts should have been installed was a key piece of evidence cited in the NTSB report:
Overall, the observed damage patterns and absence of contact damage or deformation around holes associated with the vertical movement arrestor bolts and upper guide track bolts in the upper guide fittings, hinge fittings, and recovered aft lower hinge guide fitting indicate that the four bolts that prevent upward movement of the MED [mid exit door] plug were missing before the MED plug moved upward off the stop pads.The NTSB explained that a door plug is supposed to be "secured from moving vertically by a total of four bolts." "Once these bolts are installed, they are secured using castle nuts and cotter pins. Outboard motion of the plug is prevented by 12 stop fittings (6 along each forward and aft edge) installed on the fuselage door frame structure," the NTSB said. Obviously, the bolts were never found. "The two vertical movement arrestor bolts, two upper guide track bolts, forward lower hinge guide fitting, and forward lift assist spring were missing and have not been recovered," the report also said.